I WAS
now beginning to settle down to my new life and used my free time at sea to
study for a second class Board of Trade Certificate of Competency, I had
much to learn. In November 1937, we learned that our next voyage was to
Australia via South Africa steaming outward bound on coal and returning on
oil. Most large steam ships had been using oil firing for some years, so the
conversion of the Stuart’s boilers to coal firing was perhaps unique. At
that time, bunkering oil was imported into Australia and its high cost made
it economically justifiable to change to coal firing and increase the
stokehold crew for the longer voyage.
The
normal stokehold staff on oil was two firemen on each watch (six), on coal
six firemen, two trimmers and a ‘peggy’, making a total of 27 men. So,
accommodation, food and wages for the four months voyage had to be provided
for the extra 21 men. I was told that the Stuart had made similar
voyages before, and one of the problems for the Second Engineer and the Mate
was finding sufficient work to keep the 21 surplus men gainfully employed
homeward bound.
No 2 and
3 holds were used as coal bunkers filled in the UK, oil bunkers and
double-bottoms filled at Cape Verde Isles on the outward passage. Around the
Australian coast as the coal was used the boilers were progressively
converted to oil firing, an arduous task for the ship’s engineers, in
addition to their normal duties.
We left
Liverpool on 20 November 1937 and the passage out to South Africa was
uneventful, but my learning curve was given a vertical ‘blip’. None of we
assistants, or, indeed some of the senior officers, had had coal-firing
experience and coal firemen were few and far between - No wonder when a
comparison is made between coal and oil firing for the same pay!
The two
oil firemen on each watch had to clean 24 oil burners, after which no
further physical work was necessary. Coal firing was a different ‘kettle of
fish’, it was a continuous hard slog in hot, dirty conditions for the same
pay. I quickly found that the only way to lead the men and carry the steam
‘on the blood’ under these conditions, was to be able to fire a boiler as
good as they; learning how to use the slice, jumbo-rake and shovel and to
understand stokehold terminology e.g. ‘B— ol’ man on the back-end’ and ‘on
the rattle’, etc. Also, as their vocabularies were limited and supplemented
by many four-letter words, it was necessary to be able to use the latter so
that a degree of understanding was established between oneself and the men.
When on
oil the Stuart’s average speed was 11—15 knots, but on coal it was
difficult to maintain 13 knots. The necessity to clean at least six fires
each watch meant, for the first and last hour of each watch, the steaming,
capability was much reduced. Consequently we were two days behind schedule
on reaching Cape Town.
On
Friday 17 December 1937 when the ship was nearing East London it became
foggy during the morning. When I came off watch, after 8.00am, I could see
in the distance the tops of hills above the fog bank. As was my practice, if
no ‘field day’ duties were required, after breakfast I would take a short
nap on my settee. A sudden jolt and the engine room emergency bells in the
adjacent alleyway must have awakened me. Donning a boilersuit over my
underpants and ‘chain-breaker’ vest, I slid down the flights of engine room
ladders joining the watch-keeping engineers.
The
vessel had already developed a starboard list and the heavy swell was
causing the ship to shudder violently because (as was later found), she was
firmly held on the rocks at the for’d end. The situation was frightening,
especially for the younger engineers like myself. We were fortunate having
Mr Brandie, the second engineer, who encouraged and led us with a nonchalant
approach to the serious and difficult conditions which worsened during the
next five hours. (Sadly I believe he was lost with 72 others when the
Avila Star was sunk by U-201 in July 1942.) In order to maintain steam,
the first priority was to get as much coal as we could from No 3 hold
through the watertight door into the stokehold. This procedure was speeded
up because water started pouring into the hold shortly after grounding. When
the inflow of water mixed with fuel oil increased rapidly, the watertight
door was closed. In the meantime we had been told that tugs from East London
were coming out to our assistance and that we should be prepared to give
full astern power when telegraphed.
Two
attempts to pull the Stuart off the rocks were made by the tugs with
our main turbines giving maximum astern power. The first attempt was aborted
when the tugs’ hawser parted, and the second attempt was maintained for some
time. I think for 20 minutes but was finally abandoned.
During
this time conditions in the stokehold and engine room deteriorated, the
constant shuddering movement each time waves hit the starboard side made it
difficult to maintain one’s foothold on the sloping floor plates, (varying
from 3 to 40°) as the level of oily water rose in engine room and stokehold.
Unfortunately the two steam driven DC generators in the engine room were on
the starboard side, one at floor plate level and the other about three feet
higher on a platform. Soon the water level rose above the floor plates
making it necessary to shut down the lower generator. Later the second
machine had to be switched off. From then on we had no electric lighting,
but daylight through the engine room skylight made it possible to move
around the centre platform but hand torches were needed in the wings. In the
stokehold they were essential to enable us to carry out our duties but it
was still difficult climbing up in the fiddleys to see that each boiler
gauge glass had water in it.
Pumping
the stokehold bilges had started shortly after the grounding hut despite
using all the pumping services the water level soon approached the lower
fireboxes on the starboard boiler. A dangerous situation because any in-rush
of water into the fireboxes (still filled with burning coal) could cause a
blow-back, probably blowing off the cast iron doors! It was thought that
coal/ash was now blocking the bilge suctions so I was instructed to removethe
bilge valve covers which were already tinder water and positioned just
opposite the fireboxes where the water level was only inches below!
Mr McMahon, another assistant engineer, was
with me. He was on the 12-4 and as there was a personality clash between us,
we were not on good terms. When I took over from him on watch, we had a
different interpretation on the amount of fuel left in the settling tanks.
There was keen competition between watches because the fuel consumption
showed how efficient the stokehold engineer had been with his combustion
management. He was a dour Scot and big with it! My attempts to remove the
bilge valve covers under a foot of water coated with bunker oil was not easy
by torch light and the knowledge that a minor explosion could occur at ally
moment from the fireboxes behind me didn’t help! Mr McMahon pulled me away
from the dangerous position and carried on with me handing the tools to him
from a safe distance until the covers were removed. I held him in high
regard from then on. During times of danger often undiscovered weakness or
strength of character is revealed. It was a lesson I have never forgotten.
The situation continued to worsen in
stokehold and engine room, the water level increasing despite bilge, general
service and ballast transfer pumps working full power on the bilge lines. As
the list to starboard increased the starb’d boiler was isolated and steam
pressure released by jacking (lifting) the safety valves. It was obvious the
water level in No 3 hold had increased rapidly because the resultant
pressure was causing the watertight door to leak badly and at various points
above from holes in the bulkhead. Jets of water were cascading down onto the
floor-plates making it difficult for us to avoid getting drenched. Chippy’
was sent for who managed to reduce some of the leakage by plugging and
wedging the watertight door. The ship continued to judder violently, lack of
daylight, the smell of fuel oil, the noise of escaping steam and the
knowledge that the ship could keel over any moment, provided a stressful
condition for all hands.
Sea water had now reached the centre-line
tunnel between stokehold and engine room. It must have been two hours after
the grounding when the two centre-line, single ended boilers were isolated,
de-pressurised, leaving only the port boiler in operation. It was supplying
steam to all the pumps and in addition, the starb’d Gwynne (main condenser
circulating pump), which had been put on bilge injection with the sea inlet
closed. This pump was able to suck large volumes of water from the engine
room and pump it directly overboard and at the time seemed to be holding the
level of flooding. However, by about 2.00 pm it was obvious that despite the
all-out effort to contain the in-rush of water, we were having to wade
through two feet of water when passing through the tunnel between engine
room and stokehold.
I think it was about 3.00 pm when we were
told to abandon ship because the barometer had begun to fall and when the
level of water was beginning to cover the starb’d turbine. It was then that
we assistant engineers realised a dramatic clean-up was necessary before
going topside; so we stripped off in the workshop discarding our oil soaked
boiler suits, underwear,socks/shoes and washed each other down with paraffin using rags to get the
majority of fuel oil off our bodies. It was also necessary to rinse our hair
in a bucket of clean paraffin. I took a last look clown as we climbed the
ladders, naked, cringing from the uncomfortable feel of the hot oily flings
of the gratings, I could see the compound two-cylinder engine driving the
main circulating pump still running under water! It was fascinating to see
the cranks, connecting rods and eccentrics moving under water as if on
normal service, presumably the port boiler was still supplying steam from
its residual heat and remains of burning coal in the fireboxes. (One wonders
if modern electrically driven auxiliaries would function totally immersed,
provided power were still available.)
We were
ordered to pack a minimum of clothing and personal belongings as quickly as
possible and to stand-by to be taken off by the lifeboat from East London.
It used the Stuart Star’s port side which provided a lee to the heavy
inshore swell. As we walked along the deck to disembark the extent of the
damage and penetration of the rocks into the ship’s double bottom tanks were
indicated by the bilge sounding pipes. They were pushed out above the deck
level some three to four feet, No. 1, 2 and 3 holds affected!
It was
ironic to note that the Stuart Star had come to grief immediately
opposite Hood Point Lighthouse which was only visible some twenty minutes
after the grounding, when the fog had lifted. Unfortunately at that time the
lighthouse had no fog warning apparatus because the incident of fog was very
infrequent. I understand sound warning equipment was installed after the
wreck.
The 15
passengers had been taken off during the morning and the majority of
officers and men were ashore by late afternoon. Finding accommodation for
everyone was difficult because it was the summer holiday season, hotels were
full so we junior officers were kindly accommodated in the homes of people
associated with seafaring activities. I was fortunate in being able to stay
in, I think, the harbour master’s or tug master’s bungalow. An army camp
hosted the ratings.
On
visiting Hood Point the morning after the grounding it confirmed the wise
decision to abandon the vessel because heavy seas were pounding the
Stuart, they were breaking over the decks and one could see spray as
high as the masts and funnel, getting a boat alongside would have been very
difficult and dangerous.
We spent
a few days in East London and travelled back to the UK in the lap of luxury
as first class passengers on the mv Dunbar Castle.
About a
year later after the loss of the Stuart Star, I made another trip to
Australia via South Africa, on the mv Australia Star which called at
East London. I was able to get round to Hood Point and was amazed to see the
damage to my old ship; the hull had been broken up into three separate
sections, separation taking place just abaft the main engine room and again
at the poop, the latter sections being some half a mile down the coast from
the main part of the vessel.